Tullow Oil Successful Cormoran-1 Exploration Well Offshore Mauritania
January 10 2011 - 1:50AM
Dow Jones News
Tullow Oil PLC (TLW.LN), an oil and gas exploration company
announced Monday for the Cormoran-1 exploration well in Mauritania,
has been drilled to a total depth of 4,695 meters below sea level
and has been plugged and abandoned as a gas discovery.
MAIN FACTS:
-Stabilized gas flow rates of between 22 million and 24 million
standard cubic feet per day or MMscfpd, were obtained during a test
of one of the four separate gas columns encountered by the
well.
-The Cormoran-1 exploration well is located in Block 7, offshore
Mauritania.
-It lies 2km to the south of the Pelican-1 gas discovery well,
which was drilled in late 2003. The well was drilled by Dana
Petroleum, as Operator of Block 7, using the Maersk Deliverer deep
water semi-submersible drilling rig.
-Water depth at the well location is approximately 1,630
meters.
-The primary purpose of the Cormoran-1 well was to test the
Cormoran prospect, which adjoins but lies at a greater depth than
the Pelican discovery.
-A secondary exploration objective was the Petronia prospect,
which lies beneath the Cormoran prospect.
-A further objective of the well was to provide appraisal
information on the Pelican gas discovery.
-The Cormoran-1 well encountered generally thin but good
quality, gas-bearing, sands within the Pelican Group at depths
between 3,376 meters and 3,711 meters true vertical depth subsea or
TVDSS.
-This interval comprised two gas columns, one in the Upper
Pelican Group (3,376 meters to 3,420 meters TVDSS) and one in the
Lower Pelican Group (3,691 meters to 3,711 meters TVDSS).
-Good quality, gas-bearing, sands were also encountered within
the Cormoran prospect, in the gross interval from 4,351 meters to
4,471 meters TVDSS, and at the top of the Petronia prospect, in the
gross interval from 4,660 meters to 4,695 meters TVDSS.
-Drilling was stopped at a depth of 4,695 meters TVDSS for
operational reasons (elevated pore pressures).
-The well was still in gas-bearing reservoir section at this
depth.
-A drill stem test was carried out across a 33 meter interval in
the Lower Pelican Group (3,679 to 3,712 TVDSS).
-Stabilized flow rates of up to 22 to 24 MMscfpd were obtained
on a 32/64 inch choke, the flow rate being constrained by the need
to avoid sand production.
-Substantially higher flow rates could have been achieved were
it not for this operational constraint.
-Shares closed Friday at 1331 pence
-By Zechariah Hemans, Dow Jones Newswires; 44-20-7842-9411;
zechariah.hemans@dowjones.com
RocketBoots (ASX:ROC)
Historical Stock Chart
From Dec 2024 to Jan 2025
RocketBoots (ASX:ROC)
Historical Stock Chart
From Jan 2024 to Jan 2025